summaryrefslogtreecommitdiff
path: root/tools/perf/scripts/python/call-graph-from-postgresql.py
diff options
context:
space:
mode:
authorVladimir Barinov <vladimir.barinov@cogentembedded.com>2017-02-01 11:42:02 +0300
committerSimon Horman <horms+renesas@verge.net.au>2017-03-06 11:54:26 +0300
commit5b9fd1962f605a31842371471e559407c293131f (patch)
tree7067a04d08d5b7ae5ca095cb07b081d33dc83bdd /tools/perf/scripts/python/call-graph-from-postgresql.py
parent0e45da1c6ea6b18616d95c697ecd6234bc504ef6 (diff)
downloadlinux-5b9fd1962f605a31842371471e559407c293131f.tar.xz
arm64: dts: h3ulcb: Fix EthernetAVB PHY timing
Set PHY rxc-skew-ps to 1500 and all other values to their default values. This is intended to to address failures in the case of 1Gbps communication using the by h3ulcb board with the KSZ9031RNX phy. Signed-off-by: Vladimir Barinov <vladimir.barinov@cogentembedded.com> Signed-off-by: Takeshi Kihara <takeshi.kihara.df@renesas.com> Signed-off-by: Simon Horman <horms+renesas@verge.net.au>
Diffstat (limited to 'tools/perf/scripts/python/call-graph-from-postgresql.py')
0 files changed, 0 insertions, 0 deletions