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authorTony Lindgren <tony@atomide.com>2019-10-17 16:34:34 +0300
committerTony Lindgren <tony@atomide.com>2019-10-19 01:09:54 +0300
commitc145649bf262a0614fbe5955bdffdfaba9023fce (patch)
treef945097809868d9c191f443cb4181661d62de22a /tools/perf/scripts/python/export-to-postgresql.py
parent71065d3fe82dbb2a827a081ceeca272ab7fa0905 (diff)
downloadlinux-c145649bf262a0614fbe5955bdffdfaba9023fce.tar.xz
ARM: OMAP2+: Configure voltage controller for cpcap to low-speed
Looks like the i2c timings in high-speed mode do not work properly to allow us to clear I2C_DISABLE bits for PRM_VOLTCTRL register and the device reboots if I2C_DISABLE bits are cleared. Let's configure the voltage controller i2c for low-speed mode as done in the Motorola Mapphone Android Linux kernel. This saves us about 7mW of power during retention compared to the high-speed values. Let's also change the low-speed warning to pr_info about relying on the bootloader configured low-speed values like we currently do. Cc: Merlijn Wajer <merlijn@wizzup.org> Cc: Pavel Machek <pavel@ucw.cz> Cc: Sebastian Reichel <sre@kernel.org> Signed-off-by: Tony Lindgren <tony@atomide.com>
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