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authorIgor Grinberg <grinberg@compulab.co.il>2011-05-09 15:41:46 +0400
committerEric Miao <eric.y.miao@gmail.com>2011-07-11 10:43:25 +0400
commit6c7b3ea52e345ab614edb91d3f0e9f3bb3713871 (patch)
tree9018cb559bfdb2169eed32eb5c6ea4238ae5d935 /arch/arm/mach-pxa/cm-x300.c
parent150f164ef20c2438fb845d3d90c1e2e43a674fe5 (diff)
downloadlinux-6c7b3ea52e345ab614edb91d3f0e9f3bb3713871.tar.xz
ARM: pxa/cm-x300: fix V3020 RTC functionality
While in sleep mode the CS# and other V3020 RTC GPIOs must be driven high, otherwise V3020 RTC fails to keep the right time in sleep mode. Signed-off-by: Igor Grinberg <grinberg@compulab.co.il> Cc: stable@kernel.org Signed-off-by: Eric Miao <eric.y.miao@gmail.com>
Diffstat (limited to 'arch/arm/mach-pxa/cm-x300.c')
-rw-r--r--arch/arm/mach-pxa/cm-x300.c8
1 files changed, 4 insertions, 4 deletions
diff --git a/arch/arm/mach-pxa/cm-x300.c b/arch/arm/mach-pxa/cm-x300.c
index b2248e76ec8b..8a034872ac77 100644
--- a/arch/arm/mach-pxa/cm-x300.c
+++ b/arch/arm/mach-pxa/cm-x300.c
@@ -161,10 +161,10 @@ static mfp_cfg_t cm_x3xx_mfp_cfg[] __initdata = {
GPIO99_GPIO, /* Ethernet IRQ */
/* RTC GPIOs */
- GPIO95_GPIO, /* RTC CS */
- GPIO96_GPIO, /* RTC WR */
- GPIO97_GPIO, /* RTC RD */
- GPIO98_GPIO, /* RTC IO */
+ GPIO95_GPIO | MFP_LPM_DRIVE_HIGH, /* RTC CS */
+ GPIO96_GPIO | MFP_LPM_DRIVE_HIGH, /* RTC WR */
+ GPIO97_GPIO | MFP_LPM_DRIVE_HIGH, /* RTC RD */
+ GPIO98_GPIO, /* RTC IO */
/* Standard I2C */
GPIO21_I2C_SCL,